Wednesday, April 22, 2026

Hapy not Spittin Fuel

I managed to get Hapy, the 1972 TDI-powered microbus, over to Justin to get the injection pump re-sealed this weekend. Today's post covers that adventure as well as a quick trip thru a K'Lack (2004 VW Jetta Wagon) issue.
 
Getting There
head seal complete
It has been 2 years since Hapy really went much of anywhere. Most of that time, he sat waiting for attention either in an unknown, but unstartable state or in pieces. Once I had him re-assembled with a new flywheel/ring gear and had a test drive, the original reason for him to have starting problems re-appeared: Injection Pump losing prime. I was able to prime the pump with a MityVac and then crack the injectors to get him running. And, in that way I took him on a short test drive, found some issues with the lights, etc. There remained many other issues, but at least I could get him running, stopping and had my lights so I could drive him an hour and 20 minutes to Justin's shop.
 
The night before our start-of-day appointment, I got Hapy out of the back and filled with B-20 biodiesel ($6.40/gal. same as dinoDiesel. Thanks, Trump). That morning, I filled up with coffee and hit the road. Most of the drive from West Beaverton to Justin's shop is on back country roads with few other drivers on an early Saturday morning and even fewer traffic lights. It was in the 50's (F low-teens C) and clear, making the drive very pleasant. At some point after I fixed the rear speakers, the stereo lost access to 12V so I drove in silence, a familiar scene for Hapy. The road was so easy, the thermostat never opened. I had the cabin heat on, so I may have been pulling just enough heat off the engine to keep the thermostat closed. Based on the UltraGauge, the engine temp was hovering around 180*F so running "cold". When I pulled into town off the country roads, I had a few cases of not finding 2nd gear. I noted that for followup later. When I arrived, Justin and I hung out for a bit before getting started. He has so many interesting projects all going at once, you have to absorb it all. I mean, who puts a TDI in an Audi TT while also putting one into a Rabbit pickup? Love that! The way he scraps discards and re-uses them for the basis of tools is pretty awesome too. He's even teaching himself TIG welding. Small crush, maybe. Okay, fine. He does do some impressive stuff.
 
Injection Pump (IP) Reseal
hammer mod perfecting IQ
Justin had encouraged me to get the seal kit from Cascade German, since they are local-to-Oregon, when we first set the apointment. I had already purchased the deluxe kit from DieselGeek. I didn't understand the difference. These 2 kits definitely vary in their intended purpose, so they have some meaningful differences. The Cascade German version is actually less expensive, but it includes all of the little seals usually replaced when a legit shop does the re-seal. The DieselGeek kit has far fewer seals (just the 2 on top and the head-to-base seal) and it is designed for the home-mechanic to re-seal the pump in their garage without removing the pump from the vehicle. The DieselGeek deluxe kit is more expensive because it includes specialty bits a car owner probably does not have, but are needed for the job. This differentiation is important and your case may lead you to the larger kit even if you do not intend to replace much more than the 3 included in the DieselGeek deluxe.
 
Once Justin discovered the gap, we made-do with the smaller kit. Justin replaced the top 2 seals first and then moved onto the head-to-base seal. Rather than use the included "retraction limiting bolt" and try to fit the new head seal over the top of it, the head was removed, and I held the guts of the pump in-place while Justin cleaned all the surfaces and installed the new seal onto the head. Once installed, he hooked up the VagCom and hammer-mod'd (link to Hammer Mod thread on TDIClub) the injection quantity (IQ). Justin was aiming for 6.0 mg/stk because the engine was cold (54*C).
 
The engine bay was pretty dirty, so lots of time was spent getting the IP clean before we began as well as afterwards when the whole engine got a cleaning. After it dried off a bit, we let the engine idle and we looked for leaks. None found. Justin did ask about how the starter was mating to the flywheel. It does sound loud, like it may not be meshing quite right. I'll need to remove and reinstall the starter and the starter adapter to see if I can get things to sit right. The original adapter and starter that I put in just worked for years. I would expect the new-also-stock starter would fit the same. Since this is a new adapter, that is actually designed for the application, versus one I dremel'd to fit, I would think it would fit better. It's a puzzler, but one I will consider carefully as I remove/reinstall (R&R) the starter to get it to hit the ring gear more cleanly.
 
Getting Home
If there is anything we have learned over the years about Hapy, its that he loves going places and really does not like going home. How many times have I left home and the road trip to 4 Peaks or some camping spot went great and the drive home was either very challenging or partially performed by a flatbed? Too many. This trip was no different. At first, Hapy ran great. The engine was responsive and stayed cool. Somewhere around McMinnville a charged air pipe popped off, leaving me running naturally aspirated the rest of the drive home. This served as yet another reminder to never leave home with Hapy without some tools. While the turbo is great for the overall power-band, its absence is really noticeable when trying to leave the line and get up to traffic speed. Now that it was about noon on an absolutely stunner of a day, the roads were busy where they had been empty a few hours before.
 
By the time I was approaching the Dundee Bypass, I was having increasing difficulty finding 1st and 2nd gear. Sometimes, one or the other would be right there. Other times, it was a "can't find it, grind it" experience. This persisted all the way home, forcing me to sometimes leave a stop line in 3rd. When you add in the no-turbo, I had some dissatisfied fellow travelers around me. I did get home, however, and I drove Hapy all the way into the shop so I can chase these issues.

K'Lack
After having something to eat, I switched over to K'Lack, the 2004 TDI Jetta Wagon with a BEW motor. It had been throwing a crank position sensor error, lighting up the check engine light (CEL), preventing it from passing smog. I had ordered a replacement from Cascade on Thursday, and it was in the morning mail on Saturday when I got home from Justin's. The removal/replacement of these is not complicated (remove bolt, unplug from harness, install is reverse), but getting to the sensor and the weird bolt head complicate things. The sensor sits right behind the oil filter on the front, when the engine installed transverse like normal. The bolt head is a 9mm 12-point. Half of my sockets are 6-point and the other half are 12's, designed, I think, for easier application onto hex bolts. In this weird case, that socket set perfectly onto the 12-point bolt head. With the right socket, short extension and ratchet the bolt comes out fairly easily. The plug end is fitted into a metal tang, but otherwise once unplugged, the whole thing can just get dropped through the gaps onto the ground.
 
To install, I plugged it in first and then covered the sensor with a rubber glove to lower it past the engine ick and then below the car. Could I have cleaned the engine bay before starting? Yes. But then I would have been lying in mud since the car was on my front lawn, not back in the shop and I didn't want to lay in a puddle. At this point, I found having another person to be your eyes is very helpful. I got under the car, un-gloved and suspended sensor in hand and had Boo tell me east-west, up down until I was able to send the sensor into the hole. By doing it in this order, the sensor wanted to be oriented such that the bolt holes lined up naturally. I sent the bolt thru, tightened with the socket/ratchet combo and I was done. Since I cleared the code we need to run a few cycles until it is ready to smog.
 
For the legal-minded, Oregon cops are interested in registration violations after years of looking the other way post-CoViD. K'Lack got a registration-violation ticket while legally parked in downtown Portland. Drivers beware.
 
Hapy Wrenching
Feeling confident, I switched back to Hapy, and re-connected the charged air hose. As I suspected, it was one of the rubber-to-metal bits. I cleaned both the outside of the metal pipe and the inside of the rubber with brake cleaner so they were more apt to stay together and then tightened the clamp down.
 
I next wanted to chase why the lower gears were sporadically missing. I checked the front of the transaxle to see if it was out of position at all. Nope. Right before Boo and I bought this house, I bought a Gene Berg shifter. The new-at-that-time seats were higher than stock, moving the approximately-stock-length Scat gear shift further away. The Gene Berg shifter is a few inches longer, so I figured there would be less leaning. I had not gotten to installing it before the house was bought and life took a turn. Anyway, at this point I looked at the Scat shifter I had installed, probably over 15 years ago and slid the vinyl boot up the shifter. The plastic bits on either side of the shifter appeared to be allowing more play than I remembered. Hmm. Then, I looked at the rest of that mechanism. It was very rusty, especially the foot that rests on the floor. I shot the bolts with Kroil and after waiting a couple of minutes, removed them with a 13mm spanner/socket combination.
 
rust under shifter
The floor under the shifter had meaningful rust to match the rust on the shifter foot. I don't know how much play was created by the plastic bits, nor how much may have been introduced by the rust. I do recall, however, that the Scat shifter instructions did not account for adjusting the placement of the shifter front/back nor left/right. When looking at the foot profile, it looks very much like it is designed to sit squarely in the oval without any adjustment at all. I don't know if this was a terribly good design, but I will be installing the Gene Berg shifter which does allow for adjusting. I cleaned up the rust dust, shot the floor and the shift-rod end with brake cleaner and got everything as clean as I could. Then, I painted the area with Eastwood's Rust Encapsulater (the new stuff is even better than the original) and called it a day. I still need to treat from below. I shot the picture on the right here as I was almost done applying the paint.
 
Wrap
Well, that's where we stand right now. I have been in and out of the shop a few times since Saturday and there is not a single drop of fuel on the floor under Hapy. So, we can close the book on the IP leak. I intend to complete the shifter swap and then R&R the starter next. I hope that will be the end of both issues, but I suspect there will be more to do than that. Then, of course, there are all the other things like a fuel level gauge, the radio, and the diesel heater just off the top of my head. There are many incomplete items on Hapy. Now that I have a mostly-inside (one doorway remains), concrete floor'd space to work, my desire to work on these cars has really kicked into a new level.
 
Thanks, as always, for following along and more next time-

Wednesday, April 15, 2026

Building a Shop - Doors

Ia accept that putting a garage door on your shop is barely car-content, but it is the big deal around here, and it is at least tangentially related to cars. Recall, the shop was designed with 4 openings: on the North, the big door and a person door; facing West, a barn door and facing South a to-be-determined door. I lightly described the barn door in the Ghost of GoRo. Today's post is about getting a big door for the front of the shop and all the stuff around that.
 
Before I begin, for my US readers, happy tax day. I recognize there are very curious ways this administration and his congress are choosing to allocate money, and today of all days, that "curious" feels more acute. You may not be able to influence their choices, but you can choose to vote with your wallet every day. Please direct your purchasing choices into small businesses. Those mom and pop operators are your neighbors. When you invest in them you are investing directly into your community, and not into some corporation which takes from it.
 
Measure Twice
This is so obvious and yet, this was almost my biggest mistake. When I first was designing the shop, I had the front of the shop (facing north) almost completely open for a massive door: 6 meters / 18 feet wide by 3.3 meters /10 feet tall. My thought at the time was that 6 meters would easily allow me to move 2 cars side-by-side without having to get either too deep into the shop. Like, I could have one sticking halfway out and still get a car in. This was great thinking until I decided I wanted a way to get in/out through a "man" (I say "person", but I'm not pronoun-hostile either) door. I also wanted this facing North, next to the big garage-style roll-up door. This way I could leave the big door closed and still come and go through a door with a lock on it. Consider the barn door is locked from the inside, and that was always the plan. I have no idea what the southern door will be like, but it may not have an externally-facing lock on it.
 
no wind inside
Anyway, fast-forward to after it is built and I am looking for a tracked roll-up door. After spending weeks looking for a 18' x 10' door, I have a site visit by a local door company (Overhead Door of Portland) who has a used door that big. We run the tape and sure-enough the opening is 10' high, the clearance above is adequate. Then we check the door width and it's only 16' (5 2/3m). Duh. When I added the person door, I reduced the size of the roll-up door and completely forgot. Ultimately, this saved me a bunch of money, though, because a standard residential tracked roll-up door is 5 2/3m (16 feet). When I say a bunch of money, the used door he had would have to cost me $14k US including install and an opener. The larger opening also would have pushed me into a commercial-grade door, so it would have weighed nearly double the residential door.
 
Patience Pays
open, windy inside
With the more accurate measurement, the fine folks over at Overhead Door of Portland dug into their stock of used doors. After a few weeks, they had a suitable door. Boo and I want a glass door, to maximize the light coming on for cold daytime work (think: winter weekends) and to not block overhead lights when it's open. We both also thought that a clear door would more closely approximate an old filling station look that we both had romanticals about. These glass doors, though, are less common and more expensive. The door they have is undamaged, but whoever had installed it chose to mask off the glass and then rattle-can paint the doors and rails with black Rustoleum paint. That decision would have been totally fine, had they prepared the surface for paint. At bare minimum the doors needed to be scuffed with 300-grit to 400-grit sand paper (or a red ScotchBrite pad) so the paint would have something to bite into and then wiped down. They did not and the paint did not. Instead, the paint is flaking off and is not presentable to most. For our purpose: make opening clear, yet lockable while looking old-Skool... it is perfect. We may change our minds and fix the paint, but for today, we are happy with it.
 
Car Mad Dash
Hapy's spot
As is so often the case, this was a full-on hurry up and wait. Well, really, it was more of a wait and then hurry-up. I have been looking for a door since the shop was built and now that we found one, the install was planned for less than a week later. From my prior post, you know that Oliver is against the east wall, right up against the big door opening. And, he was not running. Next to him is Hapy, barely jutting out the big opening and barely running. I needed to get both cars out the way and the lane way clear so they could get in there with the doors and equipment to get the door installed.
 
Getting Hapy out was easy: re-prime the Injection Pump with the MityVac, crack the injectors, pop the starter to a count of 5, re-tighten the injectors, start and back him out. This took less than an hour and I parked him in his longer-term designated spot where we can more easily visit and drive him. Yeah, I said visit; he's family.
 
Oliver drove!
Moving Oliver was a bigger deal, but only because I made it so. I wanted him to leave the shop under his own power. So that meant getting him running. In my last post, I described solving his fuel system. I don't know if it was insufficient patience or if I flooded the carb, but he would not start that day. A week later, and I have Hapy out of the way, I was ready to push Oliver out if I had to. First, I checked his spark plugs. They smelled like gas and were fairly black (fuel mixture probably too rich). I hit them with a wire brush and then re-set the gaps (0.033", internets recommend between 0.025" and 0.038") depending on lots of factors. I turned the key, got the fuel pump to prime and then quiet way down. At the carb with my hand, I "pumped" the accelerator a couple of times. At the wheel, I pulled the choke and tried to start him. After a few seconds, he started to act like he wanted to and after a few more tries, he fired up and held idle. This was the first time he ran since I rebuilt the carb, so an historic moment. Attempts to vary the engine speed with the accelerator pedal were fruitless, so I idled out of the shop, down the inclined gravel drive, and parked him in front of the person door. I was able to confirm that the throttle cable was junked. It would not stay on the pedal arm and then I was unable to move it consistently by hand. I'll be replacing that soon.
 
Final Prep
installers getting started
With the cars out of the way, I could get the last bits done for the door installers. I had strung outdoor patio lights around the inside of the shop, extending across the large door opening. So, half of that strand needed to come down. Last, I swept the floor which had not been really looked at since I moved the cars in last fall. With Oliver and Hapy out of the shop, I was able to really appreciate the size of my new workspace. It's really nice, and I will need to make a focused effort to leave myself room to work by not housing all of the cars inside all the time.
 
Door Install
The 2 installers from Overhead Door of Portland arrived as-scheduled around 10AM. They backed most of the way down the lane-way so the distance to carry the panels and runners was shorter. In half an hour, the doors were off the truck and positioned for installing (picture on the right). By 1130AM, 4 of the 5 door panels were installed on the runners and they were a-fixing the runners to the building. By 1PM, the door was in, the runners set, and the spring installed. Within the next hour, the install was complete, and Chris and Chase were showing us how the various controllers worked. With the door open, obviously, its almost like being outside. Well, its exactly like it was before the door was there: Full wind and misty rain on my face. Overhead, once lights are installed, the door will not block the light from reaching us beneath. That's huge. When the door is shut, the sound, wind and rain all stop. I did not expect the degree to which the air movement and sound would change. It is significant.
 
Wrap
Well, that's it for today. Next, I will be replacing the rear brakes on K'Lack (2004 Jetta TDI driven by my niece), replacing the throttle cable on Oliver and bringing Hapy over to Justin's to have the Injection Pump resealed. I don't know if any of those are really blog-post-worthy. Summer is coming, and having a safe vehicle (or a few safe vehicles) for Summer adventures starts now. As always, thanks for following along-

Tuesday, April 7, 2026

Oliver Fuel Fun

Boo had to work on Easter, so I had a Sunday to work with. Knowing others around the neighborhood were celebrating Easter with their families, I wanted to keep my noise and smoke to a minimum. So, I started slow, throwing Oliver onto a charger and then doing inside stuff. By 11, I was mowing the front lawn with the electric mower. With hand tools, I fixed the gates to the fence by lowering the little swivel wheels and re-setting the patio block they set on. Now, the gates sit mostly level and mostly vertical. By 2PM, most of the family gatherings were breaking up, so I felt I could make engine noises and such. So, I headed out to the shop. Engine noises. Ha. Such optimism.
 
No Start
fuel works
I am sure this comes as no surprise, but my first attempt to start Oliver was not successful. I really didn't expect it to, tho. I had a little over a gallon of gas in a jug that I poured into the tank, but I noticed that the fuel pump noise never lessened. So, as I walked to the rear of the car, I expected there would be no fuel in the filter. And there wasn't. The series of things the fuel needs to pass through before arriving at the pump is: fuel level sender / pick up tube -> flexible fuel line -> clear plastic fuel filter -> flexible fuel line -> fuel pump. From there, it travels, at pressure, thru another flexible line, through a short section of 90* hard line, more flexible line and then to the hard line that runs along the frame to the engine compartment. That's a lot of junctions. I started at the pump, testing with a MityVac vacuum pump, working my way back towards the tank. In retrospect, it would have been smarter to work my way forward from the tank all the way to the carb. Lesson learned.
 
Fuel Shower
upper one is bad
One of the short hoses was bad, but there was nothing visibly wrong with it. The picture on the right here is of those 2 lines. The top one cannot hold vacuum; the lower one can. This serves as a great reminder for those driving gravity-fed fuel system'd vehicles like the old VW bus. Fuel lines fail, sometimes not that long after you've installed it and sometimes you can't tell from looking at them. For a gravity feed system, you discover the leak after you've filled your tank, and it gushes onto the ground it you're lucky. Onto your hot exhaust if you're not.
 
While looking for the cause, I cracked the fuel level sender on the tank to confirm that I had enough fuel. I did. Once the one short line was replaced, I went up front, turned the key and started looking for another leak. I did not have to look very far. Immediately forward of the fuel pump, I had fuel going everywhere, running down the rear differential.
 
I concluded that it was another short hose, but noticed that the combination of short hose, weird 90* hard line, longer hose made little sense. I think I did that when I installed the fuel pump because the outlet of the new fuel pump was not clocked the same as the original and I didn't want a kink in the hose. If I remember correctly, I had already cut that longer hose, and solved the wrong problem. Or solved the right problem the wrong way. I think, that 90* bend was from the original system to go from the sender to the pump, and in this installation, I have a clear plastic fuel filter serving that function. Regardless, I corrected this time with a longer hose that runs from the pump to the long hard line. The longer hose was long enough to have a gentle arc, preventing a pinch in the line I was probably trying to avoid with the weird combo of parts. In the bottom picture, you can see that I have a small fuse for the fuel pump. This was not there stock, but I felt that with so many things living on the switched circuit, having a fuse around the fuel pump was probably a good idea.
 
Still No Start 
fuel pump
With the rear end lines set, I turned the key again, and the fuel pump quieted down after a few seconds. I looked under the car and no puddle was forming. There was not a drip at all. I went to the engine compartment, and there were no leaks there either. So, I tried to start it. No love. By now, it was approaching 5PM, and I had to get dinner started. But first, I wanted to know if the hard line was blocked or if there was fuel at the inlet on the carb. I removed the fuel line and gasoline dribbled out. Win. We have fuel at the carb. I put everything back together. Before heading inside, I checked the lights and hazards to give myself a little "well that works" energy before calling it a day.
 
Wrap Up
That's as far as I got on Sunday. After the random home-repairs, I had left myself more than enough time, had Oliver actually started, to give him a deep cleaning. That still needs doing, but first I need for him to run. I rebuilt the carb a couple of years ago, and the engine ran with it on there, so I don't think the issue is fueling, but it still could be. I will start with the spark plugs next time, and confirm I have spark. It is absolutely possible that something worked free during the move into the shop. If that does not bring me the start I am seeking then I will re-examine the carb. Maybe some gas residue became a thin varnish holding the bowl float, or is clogging a jet or something. 
 
That's all for now. Thanks, as always, for following along- 

Wednesday, April 1, 2026

Returning to Oliver

The last week or so has been busy with lots of not-car stuff. We have had our young niece over a bunch while her mom had surgery on her wrist, and a bunch of social events. Of course, with the return of spring comes the return of recurring yardwork as well. So, I have not had the dedicated time for wrenching that I always seem to think will be available. I was able to get out to the shop for a few hours on Sunday, though. I focused on Oliver, the 1978 MGB, letting Hapy ('72 VW microbus) sit until Justin has his time with the injection pump in April. The rate at which the price of diesel fuel is climbing (passed $6US/gal around the corner), I may find that it costs more to fill his tank than to pay Justin for his time. That's totally upside-down. Anyway, back to wrenchin.
 
Voltage Gauge
remember Oliver?
I installed a Smith voltage gauge into Oliver where the original analog clock used to sit. The clock didn't really work very well, and it ate voltage from the battery when I let him sit for too long. This made the clock less accurate, leading me to pull the positive cable off the battery while not in use. This led to the clock being completely worthless. So, I pulled it out and swapped in the voltage gauge. It seemed like a valuable bit of info to have, but I had wired it into the "purple" or always-hot circuit. Like the clock, the voltage gauge slowly drained the battery down, albeit not as quickly. So, again, I pulled the positive cable while not driving. I changed that on Sunday.
 
Bearing in mind that any entry back into working on cars may not seem like a big deal to regular wrenchers, but I have really not done much car stuff in over a year. So, any steps taken are a big deal. Removing the gauge was simply unwinding the knurled nut holding the rear support and the gauge flopped forward out of the dash. I removed and taped-off the "purple" wire and started seeking a viable switched "green"source to tap into. Switched is available at a few spots, but I decided to run a dedicated line from the fuse box instead. I could say I did that to remove variables or variability in the voltage signal. The truth is that Oliver is parked so close to the side wall of the shop that getting in and under the dash was virtually impossible. I was not going to just start grabbing an unplugging things.
 
Smith voltage gauge
Running another wire is simple enough. I started at the gauge and worked my way behind the dash, center console, and glove box to the firewall pass-thru. From the pass through within the engine compartment, the bundle of wires run along the left fender to the fuse box. I tied the new wire into the existing green bundle and tested continuity with the multi-meter. Success! I installed the gauge, hooked up the battery and tested by turning the ignition to "run". The voltmeter slowly crept up and I could hear the fuel pump banging away. I recall that it used to get quieter with fuel in the pump. Satisfied, I turned off the key and looked for any other parasitic drain on the battery. The wires in the engine compartment need some containment. I am not liking the scattered multi-colored angel-hair look in the picture below right.
 
Battery Drain?
technicolor angel hair pasta wiring
Testing for a parasitic drain on your battery ought to be relatively straight-forward. Disconnect one cable. Set your multi-meter to test for Amps and then place one probe on the battery post and the other on the cable end. All 0's? Switch to milli-amps and try again. According to the internets, if the drain is less than 50mA, it is not enough to drain your battery. I got 0mA, which, honestly, I do not believe. I tested it multiple times, and even after cleaning the cable and the battery post, I still got 0mA. So, I checked voltage across the 2 posts (12.08V) and left the cables attached. I figured if the voltage drops overnight then my battery-drain test will be proven faulty. I have since tested the voltage the last 2 days. The battery loses 0.02V overnight, which I think I can attribute to the stereo. Regardless, I will need to add a float charger.
 
Red Rollie
new lock, locked
I have this old red Kennedy tool cabinet we call "Red Rollie". It houses a bunch of tools, and for most the nearly 20 years that I've owned it, the lock didn't work. Well, I didn't have a key for it. We got the cabinet at an estate sale without the key. Anyway, some tools were stolen from my next door neighbor's yard a few months ago, so that changed our vector regarding the shop. We were perfectly fine using it without doors, but I can't leave entire tool cabinets unlocked if thieves have found our quiet little neighborhood. While I think the theft next door was an inside job (they run a construction business out of their home), one can never be too sure. So, I found a lock that fits this old Kennedy cabinet (Kennedy 80403 High Security Tubular Lock), and replaced it.
 
Replacing one of these locks is actually easier than on newer cabinets. The lock is held on with a U-shaped tang that slides off to the side. The hard part is you can't see anything. With my fingers I was able to determine which direction the tang needed to slide to be removed (facing the cabinet, slide right), and then set a stubby slotted screw-driver against the lip of the tang. It only took one well-leveraged push to get the tang removed and the lock to pop out. To install, orient the lock so the little inner divot on the outside facing part of the lock where the key goes in is facing down (unlocked). Set the lock into the hole with one hand while guiding the locking rod into the rectangular hole on the back of the lock. Then, push the U-shaped tang in place to hold it.
 
Red Rollie
This worked great, and effectively locked the top 2 drawers. The 3rd drawer down, however, had been bent where the little hook pokes out the back. To remedy, I got a framing hammer and a 1/2" ratchet extension and beat on it until it was more-or-less flush with the rest of the rear of the drawer. For years I wondered why that drawer always set deeper into the cabinet than the others. Now I knew. Once the drawer had been persuaded, the drawer fronts lined up and that 3rd drawer locked as well.
 
Wrap
That's how I spent my Sunday afternoon. The shop still needs the 2 largest doors, but my tools are secure, and I am really starting to get comfortable in there. For example, there was a period of time while working on Oliver that the skies opened up and it started pouring rain. I never felt it. In fact, I could only hear it hitting the trees. The insulation on this shop stops the sound of rain on the steel roof. I absolutely did not expect that.
 
That's it for today. Next week is Easter, so I may not get out to the shop for much. I hope to put a little gas into Oliver and at least back him out to where I can give him a deep cleaning. 

Thursday, March 26, 2026

The Ghost of GoRo

I have been coming off of an illness, having been sick for almost a month. Yeah, whatever that thing is going around got me good. In the meantime, we have gotten some headway on the shop doors and I got to start thinking about what's next on Oliver to get him on the road for the Summer. Today, though, is a cautionary tale about selling a car, no matter who you sell it to.
 
What's GoRo
GoRo
I'll back up a little bit first. Back in June of 2023, in my "Small Fence, Big Difference" post (link here) I mentioned in passing that we had sold GoRo, our 2009 Audi A4 to a guy down the street. We told him multiple times prior to closing the sale that he really did not want the car, that there were weird issues with the transmission, interior plastic bits were breaking off and that it was a generally crappy car. He would not heed our concerns, saying it was for his daughter, he could get the mechanicals fixed up fine, etc. There was still a couple of months left on the existing registration, and he was going to have to drive it to his mechanic, and then over to Department of Environmental Quality (DEQ) to get registered. So, Boo with her ever generous heart, let him take the car with the tags on it. We went inside and recorded the sale with the state of Oregon immediately.
 
Sales Daisy Chain
Of course, we were right. He took the car and within a couple of weeks he had sold it. But, he didn't tell us, nor did he remove the tags that we had left on there for him. In Oregon, you have a month after buying a car to change the registration. Since he hadn't had the car for a full month, he was officially in the clear, but whoever he sold it to also sold it within a few days, and we lost the handle on the ownership after that. 
 
Ticket Parade 
Why is all of this important? Within a few days after our
barn door
neighbor sold the car, we got our first of many speeding or other moving violation caught-on-camera ticket, followed by parking tickets and toll-lane charges. We got tickets from Montana, Texas, California and Colorado. In each case, we sent copies of proof that we no longer owned the car. For the tickets which came from legitimate state, county or city governments, the tickets were waived. In the case where the ticket was for not paying a toll on a "private road", the charging entity did not care that were were not the owners and could prove that we were not even in the state at the time of the violation. Instead, they sent the ticket to collections, dinging our credit. To prevent further damage to our credit, we paid that one. Most of these tickets arrived within the first 6 months after the car was sold.
 
Final Straw
This week, we got what we believe to be the final ticket. GoRo had been impounded in the City of Merced and would remain in their custody until we came down to their office and paid the bail on parking tickets. We don't care and after a while they will put the car up for auction, and it will be someone else's problem. I just hope the auction house or the City of Merced removes the license plates before handing it off to another sucker.
 
Buh Bye GoRo
barn door, inside
By the time we sold off GoRo, Boo and I pretty much hated the car. The seats were stiff like bleachers, increasing internal switches were failing, plastic bits were falling off, the transmission shifted funny, etc. It outside looked great, but wow, what a lemon of a car. The lesson here for us and for you: even if you're selling the car to your friend, remove the tags. If you are all down for the sale and want to be generous, drive over to DMV and remove the tags while your friend is getting temporary plates. Once that car leaves your possession, there is no telling what will happen to that car. You could find yourself with a big pile of tickets from uninterested parties who only want money, and are willing to hammer your credit to get it.
 
Car and Shop Stuff
I mentioned at the top that we have made headway on the doors on the shop. Recall, I have 4 openings which need closings. Over the past month, our friend Ray has built barn doors for the large opening facing west using extra siding I had added to the order for the shop so those doors could get made. It is a 10 foot wide opening, so the doors are each just over 5 feet wide. They totally look the part and glide open/shut easily. We also installed a "people door" on the north elevation or facing the farm house. This leaves a 8 foot wide doorway on the backside and the main large garage door next to the people door. I have been saving for the big door. While that doorway is a standard 16' wide, it is 10' high (just in case someone comes along with something really big, I guess). So, it is a semi-standard door.
 
On cars, I have Hapy about as ready to visit Justin as I can make him. Since he hasn't really driven since I put him back together, I really would have liked to have driven him a little more. With Diesel hitting $6/gallon around here, I all the more do not want to be driving with a fuel leak. So, his next drive will be to Justin's place.
 
voltage gauge upper right
To keep my hands busy, I have been looking at Oliver, the 1978 MGB. I couldn't get him to start when I went to move him into the shop and I didn't really look into why at the time, I just hauled him. I slid under the rear end and discovered why: I had drained all of his fuel out the last time I parked him. If I remember right, I put that fuel into the lawn tractor and the rest into Astra. Antyway, I test-fired the fuel pump with 12V directly from the battery and the fuel pump works. So, if it does not come on with the ignition key-turn, it's a wiring issue. After messing with that, I removed the voltage gauge from the dash and will be sourcing switched power for that. I had simply used the always-hot 12V for the clock I had replaced, but that runs the battery down eventually. I hope to have some time this weekend to finish the voltage gauge, put some gas in and see if I can get him to run, and idle. Then maybe I'll back him out and give him a long overdue bath and a drive-around.
 
Well, that's it for today. Keep your license plates when you sell your cars, and thanks, as always, for following along- 

Tuesday, March 10, 2026

Hapy Drives Again

It has been a long 18+ months without having a member of our family kicking around with us. But, Hapy is one injection-pump re-seal away from daily-driver status. Today, I'll go through the last little things. Again, my regrets for not taking many pictures. I have been away from fixing and blogging so I have fallen out of the habit of snapping a picture while I'm doing the doing. Also, I got hit by whatever flu thing that's been going around and was flat-backin bed-ridden for the last 3 weeks.

Clutch Adjustment
post-test drive
I touched on this at the end of my last post. I had to add an extra small spacer at the end of the Bowden tube as well as on the very end adjuster. To be fair, I really didn't need the one on the adjuster, but I would would not have much adjustment thread left if I hadn't. I ordered a replacement clutch cable and when it arrives, I will keep it under the rock-n-roll bed until I get to replacing it. I expect I will replace that cable relatively soon, but I want some fun drives before I take him off the road again, even to do something that I could do (and have done) on the roadside.
 
The standard adjustment advice is to shift the tension on the cable as felt by your foot on the pedal such that there is no engagement until the pedal has moved a good inch down towards the floor. This prevents premature wear on the clutch and/or throwout bearing. You don't want the throwout bearing riding on the clutch spindles all the time. That's noisy and introduces premature wear. What I did not recall from prior clownings on the cable was that the arm protruding from the transaxle would have so much play in it before the throw-out bearing touched the pressure plate at all. I recall it practically resting on the pressure plate, but my memory is not reliable. Anyway, I felt that the arm needed to press against the spring a little bit to get the adjustment correct. As I think on it now, that spring being engaged is what holds the clutch pedal all the way up so it's right. It just felt foreign. Honestly, it has been so long since I worked on Hapy, lots of this work has felt unusual.
 
Tail Light Show
Bowden Tube pic from theSamba
The tail lights were acting really strange prior to my first intended test drive after getting the clutch sorted. I start assessing the lights rather simply: run the hazards first. Since no other systems are involved, the blinkers ought to all light up together and turn off together. The left (driver) side was lighting up opposite from the others. When I added in simple running lights (still no key in ignition), the tail lights were a light show of blinking. I had initially thought that I did something funny with the reverse switch, but that is a simple dumb switch that allows 12V through when the transaxle is in reverse. So, I ruled that out. I concluded that the ground for the light fixture was poor, weak or virtually non-existent, causing the 12V to seek a ground though alternative paths of other not-illuminated lights, causing them to light up.
 
Getting into the Cavity 
The left (driver) side tail light is hidden behind a panel I added to offer colder air to the engine (See VW Bus Cold Air Intake). I had forgotten how much of the ugly TDI wiring was also hidden back there when I removed the panel. Anyway, first, I disconnected the cold air pipe at the last rubber coupling before the turn into the hidden cavity under the spare tire well. Then, I removed the 4 nuts holding the pipe flashing, and removed the air filter "assembly". While this was out of the bus, I thoroughly cleaned the air filter and shop-vac'd the cavity. With the air filter out of the way, I removed most of the screws holding the panel in place with a slotted screwdriver and bent the panel out of the way to access the tail light assembly.
 
Grounding
left side panel under spare
Immediately after sticking my head and a small flashlight into the space, I spotted a ground that had fallen off the grounding tab on the rear next to the light assembly. I popped that back onto the ground tab and tested the lights. There was no noticeable impact, but those grounds were probably used by something, so some other issue just got resolved.

I decided to add a ground directly from the metal back-plate of the tail light assembly to the unused grounding tab next to the one I had just resolved. I added what I call a "chair" tab splitter (because it looks kinda like a chair), that turns one tab into 2, to the grounding tab on the rear of the tail light. I re-attached the existing ground to one side of the "chair" and added a short brown wire to the other side, connecting it to the unused tab on the rear body. I then retested, and the crazy light show was over, and the left tail lights were much brighter. So much so, that I decided to add a ground the right side tail light, in hopes of balancing the lights.
 
The right (passenger) side is much easier to access on Hapy, but probably harder for anyone without a cold air intake cavity thing because the battery makes things tight. Unlike the left side, I disconnected the light fixture from the bus and hung it out the rear while I worked. I basically did the same thing as I did on the left/driver side: chair splitter, used an unused nearby grounding tab. Once reassembled, the left side did not see as significant an improvement, but I think the original grounding wire is shared between the lights so the right side was already getting benefit from what I did on the left side before I started messing with it, I just hadn't noticed during the left-side test.
 
Test Drive
At this point, I felt that I was safe enough to travel on a shared street. So, I backed out of the shop, down the lane-way and out to the street. He easily went into 1st gear and away we went. I did not have the little UltraGauge plugged in, choosing instead to use my senses to vibe the test loop. Hapy ran great. Power on demand at my foot, easily shifting from gear to gear, and getting into 4th but only barely before dropping back down. He still popped out of second when I quick-decelerated, but it was not as immediate and on a light decelerate he stayed in gear. So, there's some improvement there; I did not expect any. The exhaust was much quieter; I think some of my "wow this bus is loud" that drove to all the sound containment may have been at least in part from the broken exhaust-to-muffler joint. Facepalm.
 
The drive was not without its issues, tho. While the cooling fan and intercooler fans both came on by the manual switch, the intercooler fan was louder than I remembered. This could in part be because I couldn't hear it over the exhaust. Also, the noise of the turbo through the right cooling "ear" (behind the rear-most right side window) was unexpectedly loud. Again, this could have been masked by the louder exhaust and isn't really a bad thing. In a way, it's kinda cool and I can't hear it from inside the bus. Its only when walking around it did I hear any of these things and none of these are deal-breakers or send-him-to-the-shop things. I did notice that the dual-gauge I installed during the CoViD lockdown was acting funny (See Oil Temperature and Pressure). The pressure rose to the top and never came down and the temperature basically sat just off the bottom. I figured either the wires fell off on one end or the sender went bad.
 
Fixing Oil Gauge
left nut missing
Having the UltraGauge is great, but I really prefer just using the simple dual oil gauge. I can see if the temp is getting too high without a digital readout changing every few seconds. In fact, I have a VDO coolant temp gauge in my stuff somewhere that I have thought about adding into the dashpod and then I really wouldn't need the UltraGauge anymore. Anyway, solving the dual-gauge was fairly straightforward, starting with the engine-end. I figured that I did lots of moving things around, so simply disconnecting and re-connecting those wires to the sender would remove that variable. One quick peek, and clearly that was the problem: one of the M4 knurled nuts had shaken it's way loose and completely fell off. I ordered a set of 5 (the smallest set I could find not on amazon, and it still cost, like $15US). When I installed, I put some blue locktite on there so these don't shake off either. I was very grateful to not have to open the dash.
 
Diesel Leak Persists
catching the leak
Two years ago, when Hapy first started having hard-start issues, it was a fuel leak coming from his injection pump. Back then, there was literally fuel flying all over the engine bay. I spent time getting the top-end of the pump sealed, and that resolved the flying fuel and most of the hard-to-start issues, but it was during those months that I ground down the ring gear, putting us on the last 18 month trajectory. Also, I continued to lose prime in the pump, but without visible leaks. Now, I can see the pump dripping on the ground. So, the seal between the body and the head appears to be the problem, and its getting worse. I ordered a replacement deluxe kit from DieselGeek. Rather than do that seal myself, I have asked our old friend Justin (OldPoopie) to do it for a couple of reasons. First, he does these all the time, but more importantly, he has the computer bits to really get the timing spot-on. I expect that once the pump has been re-sealed and the timing set, Hapy will be a monster.
 
Well, that's it for today. Justin is super busy, so it will be a month or so before he can get hands on Hapy. In the meantime, I will be shifting focus onto doors for the shop, we have some house projects to chase and maybe I will be getting my hands on Oliver, the 1978 MGB. It feels like nice weather is not too far away, and taking the MG on a picnic run with Boo would be awfully sweet. Thanks, as always, for following along- 

Tuesday, February 17, 2026

Hapy Runs Again

Picking up where I left off last time, we had Hapy mostly in one piece, needing coolant. His exhaust was still in pieces, rear bumper on the ground and he had not started since June of 2024.
 
Coolant
full moon down the street
There is really no adventure here, but in the interest of being thorough, I topped off Hapy's coolant with some G40. I worked air bubbles out of his system by squeezing hoses, but they won't really fully work themselves free until the engine is running. So, after a couple more top-offs, I called it good and capped the overflow and coolant bottles.
 
Exhaust
The not-my-favorite, too-small-diameter, cheap exhaust installed on this engine all those years ago went back on. This was not my first choice, but I want Hapy running, so I'll circle-back on a new exhaust later. The old one came apart where the piping enters the muffler. I think the cheap muffler failed allowing the section of pipe to which the exhaust "downpipe" (we'll call it that: it's the pipe that leads from the turbo, but it does make it sound awfully grand) was welded to fall out of the muffler body. The weld is a good 4 inches from the end of the pipe which clearly fits inside the muffler body and sets inside an inner pipe within. I regret not taking a picture here; apologies.
 
ShadeTree mechanic'ing
So, I hung the muffler body by the support hook and then set to attaching the downpipe. There is one stud attached to the turbo that the 3-holed flange hangs on. Then, you swing the rest of it into place, square the gasket and send the other bolts (with washers) through. A 13mm spanner is needed for the lower bolt, but the other 2 can be approached with a socket. With the muffler swinging on its mount and the downpipe firmly a-fixed, I set the pipe into the muffler and literally hammered the muffler into the pipe with a rubber mallet. These parts will easily work themselves apart again, if I didn't do something. So, I went full shade-tree, and added a 1" angle bracket, screwed into the muffler and the pipe to hold it together. The picture on the right, here, tells the tale. Not a proud moment but that will all go to the landfill / recycler eventually.
 
Bumper
Feeling confident that Hapy would be a runner again very soon, I installed the rear bumper / tow hitch component. I detailed the original install of the tow hitch in Bus Tow Hitch. Re-install is not nearly as involved. 15mm socket needed. I set the hitch onto the TravisJack and lifted it close to where it would eventually sit and then balanced on the TravisJack while I set bolts. I fingered-on the left (driver) side and then the right (passenger) side, taking care not to drop the unit off the jack and onto me. I discovered that the exhaust pipe leaving the muffler hung in the way, but a solid kick with my boot resolved it without causing any damage to anything. Just needed some sudden blunt force. Once all 6 bolts were finger tight, I set the bumper where I wanted it depth and parallel-to-the rear-wise and torqued them down.
 
Injection Pump Prime
electrical connection cleaner
Any time I let Hapy sit undriven for a while, the injection pump loses prime. I believe this is because of a failing seal, but it's the one that's much harder to get to (and I don't have on-hand). So, I have let that sit to be solved another day. Enter the mighty MityVac. Since I disconnected the large fuel filter for the flywheel replacement, I was unsure if that filter was completely full, so I started with the line which enters the injection pump, moving to the return side of the pump next. This is relatively straightforward: disconnect the fuel line, apply vacuum with the MityVac (using the collection bottle between the pump and the fuel line, of course) until the collection bottle consistently gets fuel. Then, remove the vacuum contraption and reconnect the line. For the return line, I also clamped the return line from the injectors to the pump so I did not lose vacuum through them. Once the pump was full, I cracked the hard lines at the injectors with a 17mm spanner. This last bit of priming needs to be done by turning the ignition and counting to 5. Well, that's how I did it. When I returned to the engine compartment, each of the 4 injectors had some fuel sitting on top where the hard line connected. I snugged them back tight.
 
DeOx-it D5
Before I ran to the cab to give the engine a try, I wanted to make sure all of the plug-in bits were set. So, I went around the top of the engine, disconnecting, shooting-DeOxit D5 into the connectors and clicking them back together. This served 2 functions. First, a simple survey of the top of the engine allowed me to see if I had missed anything. Second, every electrical connection was confirmed a good-click connection and it was cleaned/deoxidized for a better connection. Having done this, and it only taking literally a minute, I intend to include a similar final survey when doing top-side maintenance going forward. Its so easy, and removes many possible variables to failures.
 
And Then It Happened
At this point, I felt that I had done everything I could to set up for a successful first start since June of 2024. I put the trans-axle into neutral turned the key to run and saw the familiar lights. With an inhale, I turned the key to start and after about 3 seconds he fired up. I didn't expect immediate, since fuel still needed to get pushed down into the injectors, but he started well and ran strong, arriving at a comfortable idle almost immediately. I left him run for a while, sitting in my shop in neutral while I checked for leaks and drips. There were none, which was little short of a miracle.
 
I thought about giving him a little test drive, but I have not solved for the electrical cord for the FrostHeater yet. Curious, though, I tried to ease him into gear, but he wouldn't. Knowing that he easily moved in and out of gear when the engine was not running, I concluded that the clutch cable needs adjusting.

Clutch Adjustment
This adjustment took a little bit of effort, but with a thicker spacer where the Bowden tube meets the mount on the transaxle, and another spacer on the adjuster, I was able to get the clutch to engage and disengage properly. The Bowden tube needs a curve in it to reduce clutch chatter, so this was needed regardless. The fact that I needed a spacer on the adjuster tells me that the cable that I replaced.. jeez.. almost 20 years ago... may be stretching. This is often a warning that the cable will fail soon. So, time to order a replacement.

I used a Velcro ties to hold the FrostHeater cable up and out of the way. But, before I wrapped it up, I tried the FrostHeater, and I think it might be broken. I'll have to do some research, but I expected the unit or at least the top hose to warm up to the touch a little bit. I did not notice any warming, so that effort may have been for nothing after all. Again, I will look into it and I may get a replacement unit, but I'll be pretty bummed if it was really only used a couple of times before it got damaged.

Here's a video of him running, probably 3 minutes after his first start in like 18 months.
 
 
 
I noticed that the rear lights were acting all weird, but a different kind of weird than usual after messing with the battery. So, I did not want to risk a drive-about. It seems like every time I touch the battery, the tail lights short-out such that stepping on the brakes completes an unexpected circuit. That's the usual. This time, the reverse lights were lit up and the blinkers were acting all strange, but only the rear. I think I may have done something with the reverse lights, like reversing the plugs when I wired up the switch, but I ran out of daylight before I could get after it. I'll diagnose and attempt to fix it next time. 

Thanks, as always for following along, and I'll post with any test-drive observations, and other improvements as they happen. At this point, I am thrilled that Hapy self-starts and can move around again--

Tuesday, February 3, 2026

Hapy Gets a FrostHeater

Today, I nearly complete the re-assembly from the flywheel (well, ring gear, really) replacement that has been an open effort since US Independence Day. I had to order a clip to hold the coolant temperature sensor in the coolant outlet flange, so this post picks up where I left off after placing that order. Before I begin, hapy belated GroundHogs Day or Imbolc, if you're a little less western in your seasonal outlook. Either way, there's 6 more weeks of winter because Spring Equinox is still 6 weeks away no matter what a Pennsylvania rodent sees. Anyway...
 
Some History 
installed
For background, Hapy was having increasing trouble starting over the past 2 years. I thought I was getting poorly manufactured starters because every time I replaced one, he would be okay to start for a few times. That was until the last couple, including a new highly-recommended starter from IDParts and a fresh local rebuild of the original TDI starter by a very reputable rebuilder. I concluded the teeth on the "ring gear" or in my case the teeth on the flywheel since this flywheel was one formed unit, had broken off enough that the starter teeth could not engage. This started a path that started with removing the engine-transaxle on my falling-into-pieces driveway, having the transaxle fall off a jack and popping off a flange, hauling Hapy in a sketchy way back to the shop, and finally, now, almost completely reassembled. When this saga completes, he would have been not running since July of 2024 (when we drove home from the final 4Peaks Music Festival).
 
FrostHeater
Frostheater is a vendor who uses a widely available Zerostart 3309040 coolant heater with hoses and brackets for a custom fit for various makes and models. If you have not tried one and are tired of cycling your glow-plugs multiple times before you can start your diesel in the winter, I suggest giving them a look. The unit Frostheater uses looks to be the top of the line from Zerostart in terms of build, capacity and cost. There are plastic other brands, and block heaters that are effectively a glue-on heating pad, but I have found these FrostHeaters to be really effective. From what I can tell, there are no moving parts. By placing the unit near the lowest point of the oil cooler loop the unit draws colder coolant from the oil cooler and the warmed coolant flows up through the upper bib into the head. That rising heated coolant then puts pressure on the coolant in the block to move into that vacuum, through the oil cooler and the loop completes. A few years ago, I installed a Frostheater into a 2004 VW Jetta Wagon (K'Lack). It worked great. We sold K'Lack to our niece a few months later, and she never used the heater. So, when we had to do a major timing belt and cam shaft maintenance, OldPoopie removed the FrostHeater, and restored the original coolant line which I left in place when I installed the Frostheater. The Frostheater and related hoses went into a box for future Hapy consideration.
 
Coolant Temperature Sensor
#6 in diagram
Before I get too far ahead of the story, I installed the coolant temperature sensor and retaining clip first. That sentence is easy to type, but the actual install is very unpleasant. In Hapy, the coolant outlet flange sits behind the fuel tank and barely above the top of the body cross-support that also contains the center-mount for the transaxle. So, there is no way to insert the clip from below, it must go in from above. Directly above the insertion point for the temperature sensor, however, is the to-the-heater side of the coolant outlet flange, leaving a 1/4" or so to fit the clip. Since the orientation of the clip is straight  up and down, there is not enough room to simply slide it in. Of course, let's not forget that you can't actually see anything because it is all on the front side of the engine. For the ALH-TDI engine install into the bay-window bus, I believe this is the single issue that challenges the install. It is minor, in the grand scheme, but it is still highly unpleasant when you need to replace this sensor.
 
So, how do we do this? With a fingernail, I find the slot on the far side (front) of the flange where the one side of the clip will go, and send one "leg" of the clip into that slot while holding the sensor firmly in place. The clip will flex hard, and the inner "leg" of the clip needs to bend somewhere while the first notch of the clip is slid in, I found that having it flex away from the flange (towards the sensor) gave me something to work with. Once the clip is most of the way down and it seems like the clip can't possibly flex any more, push the flexed inner "leg" towards the flange until it clicks into the hidden slot. I spent a couple of hours wrestling with this, and broke a clip along the way, but this method does work. These clips are inexpensive, so buy several when you need to install one. Also, I found it much easier to access the coolant flange from the driver side (the sensor side) if the charged air hose is removed.
 
FrostHeater Install
where fits FrostHeater
I could have stayed on target at this point, filled the system with coolant and started test firing the engine. In fact, I try to follow that pattern more recently: finish what you started, then do the next thing. In this case, I had already lost the coolant from just below the outlet flange and above. I figured swapping out one hose for 2 with the coolant heater was not a significant scope increase when compared to the effort to open the system to add the heater later. I figured adding it later could be years away.
 
All of the install drawings and instructions I was able to find gave very model-specific directions. I was able to determine through loosely related searches that the life of the heater is significantly extended if it does not suffer the constant vibration of being attached to the engine block. So, I looked for a place along the right side of the engine bay where it would be low enough to be nearly the lowest point relative to the engine block while still being reachable by the hoses I had on-hand. That area has a small wire bundle, the main 12V line and the diesel fuel lines, so my placement will need to be careful, but there is a section a few inches front-to-back where it could go. With that general placement decided, I shifted to hoses.
 
The BEW TDI hoses that were part of the FrostHeater kit are not an exact fit for my early ALH TDI. The top hose (red line in the drawing on the right), which runs from the top of the heater into the head hose bib which protrudes on the oil cooler side of the engine just below the coolant outlet flange (#11 in drawing), had an extra bend at the far end that I trimmed off. I felt that the extra bend made the hose want to have a large arc which would have created a hard-to-manage air pocket -or- it was a kinking risk, reducing the coolant flow. The lower hose that runs from the lower bib on the oil cooler to the lower bib on the heater simply would not work for where I could install the heater and still use the upper hose. So, I decided to reuse the hose I had originally running from the oil cooler to the head for the lower hose from oil cooler to heater (blue line in drawing).
 
viewed thru top hatch
Now, we get to hard-mounting the heater to the engine bay. The BEW install bracket on top of the heater unit was oriented to mount to the left side of something. I don't remember what. But the bracket could be easily removed with a 7/16" socket and flipped over, aligning the bracket for a right-side install. Flipping the bracket also placed the heater about an inch lower and set the angle of the bracket against the lip of the engine bay, offering some additional support. With the hoses attached, the heater unit had a smaller range of motion for deciding where to mount it without putting stress on the hoses. Still, I was able to find a spot where the bundle of wires and everything else would not get bound beneath the bracket, and marked it with a sharpie. I planned for and then drilled for a M6 rivnut. The M6 was considerably smaller than the original, but the heater is super light and I was fairly sure that bolt was designed to go into a pre-existing hole. I say "planned for" because once I got the hole drilled, there was no way I was going to be able to fit the hand-riveter into the engine bay and set the rivnut. So, instead, I simply sent the bolt through and nutted from behind like most things. It is still a M6 bolt, using washers, of course, just no fancy riv-nut. So, to remove, I will need 2 wrenches rather than one. Not a big deal.
 
Fill 'er Up
from behind approx level
With the cooling system seemingly buttoned up, it was time to add coolant and burp out the air bubbles. This is where my effort ran out of supplies: no G40 coolant on hand. I added some water to confirm there were no leaks, and after shifting the upper hose clamp on the FrostHeater, there were not any. In the picture on the right, here, you can see how well tucked up and out of the way it is, even though it is below the oil cooler. Note the dry, albeit stained, concrete floor underneath. No leaks.
 
I still need to solve for the routing of the electrical cord so it can be reached relatively easily on a cold day, but far enough out of the way that it is not subjected to flying gravel and road debris. At this point, I am looking at tucking it up behind the right rear wheel, under the battery tray and holding it in place with a strip of cable-management Velcro.It might be time to consider mud flaps back there to help protect the cable from tire kick up.
 
Last, when I removed the exhaust at the start of this project, it came apart where the pipe meets the muffler. To be honest, I was never terribly pleased with the exhaust that was put on there. But, it did last 15 years, so I can't complain too much. Still, I have a 2" exhaust kit that is a bunch of straights and turns that I intend to eventually cobble together into a better exhaust. I think, to get Hapy on the road, I will put the existing, falling apart system back in. Then, I can plan for the 2" exhaust as a near-future improvement.
 
Thanks, as always, for following along, and I intend to get coolant this week and get Hapy running next weekend.