Thursday, May 14, 2026

Building a Shop - Construction Permit Complete

For a project that started in December of 2024, I am surprised it took so long for the shop to reach "complete" for it's initial build permit. Today, I'll review some highlights and touch on a Hapy adventure.
 
The Doors
shop permitted
I had an entire post about the doors (See Building a Shop - Doors) where I detailed almost buying the wrong size big door. Then, we got things right. That big door faces north. Next to it, our contractor guy Ray installed a basic HomeDepot-special 36" (1 meter) wide person door. That door is the only door with an external-facing lock. Moving around to the west side, we have a 10-foot (3.3m) wide opening. In the Ghost of GoRo post, I mentioned the west-facing barn doors that Ray built. I will give them more detail below. The southern opening also got a barn-door style install, though the actual doors are a little different.
 
Ray's Custom Doors
barn doors by seating area
I'll start with the west-facing big barn doors. First, we sourced an external barn door rail system (~$300US) capable of supporting a few hundred pounds. The opening had a double header, so most of the rail was mounted to that, through the exterior skin. In order to create sufficient space for a door to hang, the rail install includes a small block of 2x4 between the rail and the outer skin at each bolt-point. The header only spanned the opening, so on either side, from the inside, Ray added a 2x4 on the inside for the mounting to attach to. The south-facing smaller doors had a similar barn rail system installed. We followed the pattern of using 2x4 blocks to create the offset, and using 2x4 planks inside for the mount to attach to. Unlike the west-facing door, the south-facing did not have a double header, so the entire rail needed the 2x4's installed.

southern doors
With the rails in, Ray shifted to construction of the doors. All 4 doors were framed with Sun-wood. This is exterior-qualified wood, but lighter than cedar and not chem-y like pressure treated. Because the west-facing doors are bigger, they were assembled with brackets to hold them square. And, they had angled planks added for strength against twisting or flexing. The south-facing doors were joined with biscuits, and did not have the angled planks added. Once the frames were ready and test fit, the west-side doors had siding attached so they match the building. The southern doors were skinned with clear plexiglass. This will allow the little bit of winter light we get from the southern sky to leak into the shop.

Once the doors were assembled, Ray re-hung them, and installed interior grab handles to operate them. On both sets of doors, we added guides into the concrete so the doors would not move away from the building while in place or traveling. Last, I added a lock to each door so they could not be opened from the outside. I need to prime and paint the south-facing doors, but they are operational as-is.
 
Inspected
southern doors
When I had the building inspected in August of 2025, the inspector asked for 2 things: install the doors and add a landing for the person-door. With the doors now complete, and the landing added in September (See Building a Shop - Steel Building Erected), I was ready for an inspection. So, on Monday I ordered the inspection. The inspector checked the boxes on Tuesday and now I have an officially completed building (per drawings, spec's and inspections). What does this really mean? Well, in terms of the permit and inspections, it means I get to pay taxes on the land improvement, and my home owner's insurance just went up. It also means that anything contained within that shop is now covered under my home-owner's insurance and if something catastrophic happens to the building, I'm covered insurance-wise.
 
What does this mean in terms of my personal use of it? Very little, frankly. I needed the doors so I could lock it. Once lockable, I can start storing tools out there, so I can work on a car in the shop and not walk the 40 meters from the shop to my tools in the garage and then the 40 meters back again. I have already repaired 3 cars in that shop with a 4th (Astra needs her alternator replaced) heading in on Friday. having a lockable shop means I can do that work that much faster because my tools will be right there.
 
Retrospective
where we began
Being an advocate of both Agile and Continuous Process Improvement (CPI), I believe that some kind of look-back when a project reaches its end is healthy and helps you and others make better decisions in the future. So, with that in mind, what did I learn that I haven't already mentioned?
 
     Permits: I covered most of the discoveries along the way in the linked permits post. Get Clean Water Services involved early and make sure you manage both erosion during the construction as well as any mud getting tracked into the street. Either can got your job flagged and then things get much harder.
 
    Survey: The "106" inspection is all about proper placement of the building relative to your plan and the property lines. If you don't know where your lines are and can't figure it out, you will need a survey, or you may not pass the first inspection. I split this inspection into 2 visits, with the first being informal wholly focused on the site location. This was Vai-the-concrete-guy's idea and he was 100% right.
 
excavated
    
Bidding: get lots of bids. I had 3 and had I gone with one of them, it would have cost me ~$5k more for the flatwork. Part of every conversation about the flatwork included a conversation about the excavation. For every bid, the excavation was a meaningful amount, even though it's not terribly time consuming, especially for out project. This might be something we could have done ourselves, but the schedule worked out better having Vai do it all. Last, make sure every bidder fully understands all of the parts of the plan. Vai had a brain-fade about the carve-outs for the lift and had I not asked about it after they ran the compactor, there could have been an issue. This served as a reminder that without a designated general contractor, YOU are the GC.
 
    Inspections: While Clean Water Services did verify that the erosion control measures were in place, and made sure that the storm outflow was planned for, the adherence to that plan was not in any inspection.Does this mean it isn't needed? No, nor does it mean that it won't be part of your project, it just wasn't part of mine and I managed the storm water with french drains once I was unable to attach gutters. So, I have a rock pit in my yard without purpose. The inspector can be your friend. Case-in-point, I would not have even known about an "Ufer" if the inspector had not mentioned it and then approved it. I now have a passing-electrical ground because of the inspector.
 
cleared and framed for concrete
    Concrete: I asked the concrete contractor specifically what, if anything, I needed to do once the concrete was poured. He said "nothing", and I got surface cracks because it did not cure uniformly. The correct answer is "try to keep the surface wet with a garden hose for a couple of days". Then, the top does not dry too fast relative to the concrete beneath. 
 
    Oregon Carports: these folks were great from start to finish. They were easy to work with, the plans were spot-on for the permits and inspections and the installers were fast and nice guys. It would have been nice to know that a gutter could not be installed without retro-fitting, but at this point we have weathered a full wet season easily.
 
    Driveway: When I planned the shop, I knew that the ground sloped downhill south to north but I did not account for the west-to-east down slope. Topology matters. After the steel building was up, I had over 1/3m (an American foot) drop off at the southeast corner. This led to many hours of hauling and spreading rock. Since my labor is free, this did not factor into final costs, but it may factor into your plans.
 
    Overhead Doors of Portland: Similar to Oregon Carports, the overhead guys were great to work with. They found us a door that just smashes for less than half of what I would have paid for new. They stopped by late last week to install a header board over the door and install the weather seals. Both after my check had long cleared. We will be using these guys again.
steel skeleton
 
    Ray: Ray is a star. He has been a contractor building things since he was a teenager. Now, he's getting near retirement and is not taking on any new customers. So, those of us lucky to have worked with him in the past are blessed to still have him, at least for a little while. One of Ray's greatest strengths is looking at a project without filters. He can imagine what you are looking to do and make it happen. He built the barn doors, yes, but he also built our kitchen with salvaged cabinets. 
 
Timeline
For history's sake, and in response to my "how did this take so long?" question above, here's the time line for the build, start to end. There was a break in the action over the winter Oct2025-Mar2026 while we financially recovered a little bit from the costs incurred so far. We needed to get onto Ray's calendar and figure out the doors a bit too.
 
2024-AugustBoo and I decide to build a shop and figure out about where we want it
2024-December: steel building ordered from Oregon Carports
2025-January: permit started with Washington County (WC) ($700)
2025-March: Clean Water Services (CWS) involvement in plan
2025-April: permit accepted, initial payment of ~$1k
2025-May: self-performed survey, soliciting concrete bids; locating and placing "straw wattle"
2025-June: CWS inspection, excavation, WC site inspection, concrete poured, WC "106" inspection 
2025-July: steel building installed on foundation
2025-August: french drain install around foundation, WC "199" inspection fail
2025-September: rock and gravel of drain, north-side access
2025-October: move 4 cars before rains hit
-- work suspended to save some money -- 
2026-March: west-side barn doors, north-side person door installed
2026-April: north-side overhead door installed
2026-May: south-side barn doors installed, WC "199" inspection pass
 
Costs
Similar to the timeline, I'll detail the costs as I can find them. Of course these were all in as-of-that-day US$. With TrumpTarrifs and trumpflation, your numbers may vary widely from these.
        0: Advise from WashCo, inspectors and Clean Water Services
  1800: Permits with Washington County
23000: steel building from Oregon Carports
15500: excavation, framing, concrete pouring, incl $500 for the concrete pump rental
  7500: north-facing big door from Overhead Door of Portland, incl install and opener
  4800: all other doors, incl hardware, custom build, installs
    800: french drain materials, gravel
    500: large rocks for storm outflow
53900: TOTAL
 
From these numbers, I conclude that when you think about building a shop, the cost of the building itself could be less than half the overall costs. I paid more for permits than I did for rock and gravel, which is also interesting. The 4 doors cost almost half of what the overall building cost too. I could have had fewer openings, or installed a solid overhead door to lower costs, but I'm glad I didn't. Also it is worth noting that this shop has no electrical yet. I expect that will be a 5-figure as well since I will need a trench to run power, a panel, and then lots of cabling contained in conduit. Eek. I do not expect that work to take place any time soon. Instead, I will operate with a long extension cord from the house for as long as I can manage.
 
Hapy Shifting
In my last post, I celebrated Hapy shifting so well. That turned out to be premature. The next day, I lost the ability to put Hapy into gear and had to limp home in rush hour from around the corner.. in 3rd gear. One hot clutch later I was back in front of the garage and there he sat for a few days until I could get a look at him. Of all the things that could come apart, I did not expect the bolt going through the pin in the shift linkage at the front of the transaxle. In the image on the right, it's the screw in sub-component "P". I expected the grub-screw ("R" in the image) to have fallen out because I could not remember if I had run the bailing wire through or not. Turned out I did, and the grub screw was doing fine.
 
shifter diagram
I pulled the pin out and rummaged through my drawers of fasteners and found a 11mm bolt that fit. After around 20 minutes of wrestling, which consists of slightly moving the shifter in the cab, getting back under the bus, test fitting and repeating until you can muscle the pin through the hard plastic bits in the cage AND through the end of the linkage running from the front. This time, I put blue thread-lock on the bolt added a washer and sent it into the pin. I torqued it down as best I could considering my body position and the lack of something firm to grab on the opposite end. I used a pair of pliers to hold it.
 
Hapy is back to shifting normally again.
 
Wrap Up
After Ray finished the doors and I had locks on them all, I sat in one of the rear seats from C's new mini-van / stealth-camper we set in the shop as a seating area. I took a moment to just absorb. We so often will not take those minutes, choosing instead to rush off to the next thing. I sat for a few minutes, radio playing softly in the background and simply looked around at my shop. I really can't believe it. After so many years of lying in puddles, sliding on my back on wood chips or just outside in the rain, I cannot imagine what it will be like to work inside, on a hard dry surface come winter. Even now, as we head into summer, I will be working in the shade, on cool concrete, not hot tarmac. Of course, between then and now, I have a great deal of stuff to move and organize, but as of today, the shop is open and I can't wait to get out there.
Thanks, as always, for following along- 

Tuesday, May 5, 2026

Hapy Test Drives

Quick post today.
Before I start, Happy Cinco-de-Mayo. Our US-resident Latino friends and neighbors have had a brutal 18 months since the regime started incarcerating people in concentration camps around the country. This year, I hope there is more focus on the positive impacts of the Mexican culture and the negative impacts the ICE sweeps have had than on beer sales. While I'll probably be tipping a tequila this evening, I am not turning a blind eye to the perils our Latino friends are experiencing.
 
Hapy Drives
spring flowers
This past weekend, I had multiple shows I was asked to play, so I did not get into the vehicles much at all. Since I swapped things around, I did drive Hapy to both performances, though, so I got some quality test drives in. First, I sat in with a bluegrass outfit at a outdoor new food cart venue near Tannesborne. This was mostly surface streets, so I never got out of 3rd gears, but it was over 20 minutes each way. So, I was able to see how well he performed. As expected, he ran well. On the way home, dark had fallen, so I was able to prove that his lights were all working well too.
 
My other show was at a different food cart venue, supporting Brenda (find her here). She plays guitar and has an incredibly clean, clear voice. Anyway, that venue is in Hillsboro and rather than take the long slow slog out Tualatin Valley Highway (lots of traffic and traffic lights), I took the back country roads. This allowed Hapy to get up into highway speeds. Again, he drove great, had plenty of pep in 3rd and 4th gear. Even with the bigger nozzles and the CPU-tune, he is slow off the line from dead stop and doesn't really get his wheels going until we're over 2k RPM in 2nd. I recognize he's a loaf of bread getting pushed by around 120hp but I expected more, I think. I recall the test drive after the Malone tune, but as I re-read that (See Malone Tuning, Stage 2) post, again, Hapy really looked alive above 25mph moving into 3rd. 
 
MAF check-engine code
One thing worth noting, though, is all of the small improvements to his handling are really making a difference. Recall, the rear sway bar, but tightening the rebound on the shocks, replacing the tie-rods, the steering dampener, adjusting the steering box... for that matter we could go all the way back to my first few posts 20 years ago, like this one. Now, as I drove on country roads like a local (read: fast), Hapy holds the road, a cross wind doesn't impact as much and I don't arrive completely wrung out from stress. Again, he's still al oaf of bread so a cross-wind will move him more than a normal car, but its not nearly as bad as it was.
 
By the time I was starting Hapy for the drive home from the 2nd show, the starter noise when engaging that we heard over at Justin's place had disappeared. Perhaps the starter needed to wiggle itself into position a little bit. I don't know, but I will be sliding underneath to make sure the nuts and bolts are fully torqued down. 
 
Shop Locks
boost check-engine code
Other than than 2 shows, Boo and I mostly took the weekend off from projects. I did carve out a couple of hours to put some barn-door locks on the west-side barn-doors so they can lock from the inside. This will keep casual thieves out. I say "casual" because if someone wanted to smash-and-grab, there's plenty of smash-able glass. As I mentioned last post, Ray our contractor, is building some mostly clear barn-style doors for the southern doorway. These will move all the way outside of the door frames, leaving enough room to drive a car through, allowing us to move cars all the way through and into the "back 40" where I may need to store a car or 2 while working on others.
 
Wrap
I know there's not much in today's post. The big take-away is Hapy is absolutely operational now. He is driving great, starting immediately, etc. Of course, no adventure with Hapy is complete without something happening. As I was leaving the 1st show, Hapy threw one code (P0101: Mass Air Flow sensor) and has another pending (P1550:Solenoid Valve for Boost Pressure Control (N75) - Control Deviation). We have seen the P1550 before (See: Resolving the Stammer) and know how to resolve it, if it appears again and throws a legit code. For the MAF, I'll probably try to clean it first. Worst case, I need to replace it.
 
That's it for today. Thanks, as always for following along- 

Friday, May 1, 2026

Hapy Shifting

In my last post (Hapy not Spittin Fuel), I described a stressful drive home without turbo and then losing access to my 2 lower gears. Today's post covers the install of the Gene Berg shifter, and some other little bits on the bus as well as the replacement of the throttle cable on Oliver the 1978 MGB.
 
Before I begin, especially to my union brothers and sisters, Happy International Labor Day. Employee protections were and remain hard-fought; from a legally defined "work week" to overtime pay and safer working conditions, we have our unions to thank.
 
Throttling Oliver
Gene Berg shifter
I'll start with Oliver, even though I did this cable replacement in the middle of the Hapy stuff. Recall, I moved Oliver out of the shop so the overhead door crew could install the door. At that time, I got Oliver to start, mostly by cleaning and re-gapping his spark plugs and otherwise being patient. Since Oliver does not have a stock carb set up (side draft SK Racing carb), the stock throttle cable is not an exact fit. The old cable had a much longer hard "pipe" to fit the cable through near the carb than the stock one I had ordered. I thought about simply removing the braided cable and sending it through the old sheath, but the points where the plastic sheath met the hard pipe was failing. I think the way the hard pipe was attached to the carb was a little hinky too, so the whole cable, hard pipe combination went in the bin.
 
Both the new and old cables attached to the pedal the same way: round ball on the end of the cable fits into a nook on the underside of the pedal. So, once you pass the cable through the slot, the springs on the carb effectively hold the pedal up through steady tension through the cable. The other end of the stock cable has a fitting on it which presumably fits onto the old carb with a c-clip or similar. I had to cut that off so I could thread the raw cable through the more common hole with a bolt model. Cutting the cable left wire shrapnel at the end, so it would not easily fit through the hole. Ultimately, I had to remove the actuator arm and the spring arm from the side of the carb so I could more directly feed the wire into the hole. While this was more destructive initially, I was getting nowhere trying to send a cable through a hole I could barely see.
 
One the cable was through the hole and bolted down tight enough so it would not fall off, I put the arms back, and re-added the spring. I got Boo to sit in the driver seat and move the pedal through it's full motion so I could set the depth of the hard tube and the cable length. I had other things to get after, so I did not test fire and drive Oliver. In retrospect, that may have been a missed opportunity.
 
Gene Berg Shifter
shifter diagram
I don't know when I first installed the Scat chrome shifter into Hapy. It seems like it was always there, so it may have been one of the first things I did. Back when I first bought Hapy, he did not want to go into gear at all because the shift coupling at the front of the transaxle had lost the little plastic bits. Note the picture on the right, here. In sub-component "P", there are 2 rectangular things. Those are the plastic bits which were gone when I bought the bus. If you threw the shifter in the direction of the gear you were seeking often and hard enough, the long-ish bar thing (top of sub-component "P") would move the cage (center of sub-component "P") and eventually you might find a gear. The prior owner had beaten on the original shifter so much, it wasn't straight anymore. It was literally bent. Once I got the cage resolved, the bent shifter was just too strange to use, so I bought the upgraded shifter. Or at least it was. Over 15-20 years of use, I think it slowly may have moved, though there is no facility to adjust it -or- the limited-throw bits wore down over time. Since most folks think somewhat highly of Scat products, I'll assume it wore down or moved over the years. I will say that in recent years, Hapy has predictably popped out of 2nd gear every time, and I don't remember when that started.
 
greased up
The loss of both 1st and 2nd gear on the drive home was enough for me to do something drastic. After removing the Scat shifter and discovering the rust and what looked like some wear on the plastic bits, I decided to find the Gene Berg shifter I bought a few years ago. The Gene Berg shifter is simply bad ass. It is 3 or so inches longer (Scat is 21 inches, Gene Berg is almost 25) which puts the shifter in my hand without having to bend over like I did with the Scat after adding the Sprinter seats. The picture at the top shows how high it is. One drawback: when I put it in first, I hit the rear of the cup holder. The reverse lockout is a button on the side rather than a "T handle to pull up on. I like that better too, since there is less to think about and backing up a bus requests all of the focus you can. It uses a shift plate like item "D" in the diagram above so for the more stock-familiar, this vibes well. Perhaps the most important, the attachment of the pieces has adjustment capability engineered into it.
 
I test fit everything first, and finger-threaded the supplied bolts into the respective holes, just to be sure everything would fit. Then, I took it apart and greased everything: the ball, the slides, the shift plate, and the cup the shifter tip sets into. Then, I installed it again. One thing about a test fitting is the second time around, you know how it all goes together, making the final fitting much faster. Because of the adjust-ability factored into the shifter, it was easy to wiggle the shifter and the mounting footing to get it seated squarely and threaded snug. I tested the movement of the stick and did not feel a need to adjust it. I figure after some longer test drives, I will know for sure and then execute the minor adjustments. For now, though, I fired up the engine and backed Hapy out of the shop and drove him up and back on the laneway. At this point, I have all my gears.
 
Seasonal Scrubbing
I ended my weekend of yardwork and playing on cars by giving Hapy his spring cleaning. I have documented this in the past, but in brief: I use SoftScrub bathroom cleaner and a soft brush to clean the fiberglass top. This gets all the black ick from organic material removed. Prior to this step, I will clear out the luggage rack of leaves and such. It was especially bad this year so I need to circle-back, remove the rack and clean the metal top. Once the top is SoftScrub'd, I wash the entire bus (top again) with car wash like any other car. The end-to-end process takes 2 or 3 hours, but if the sun is out and it's not too hot or cold, it is a great way to spend a Sunday afternoon. I hope to get the luggage rack removed and the tin-top cleaned next weekend. That will also give me the opportunity to repair any part of the luggage rack which needs attention. In the meantime, I swapped the vehicles around, setting Hapy up as my daily driver and the lower mpg truck for specific-use-only. As of May 1st, regular 87 octane gas is $5.70/gallon here, and diesel is $6.20 but with the mpg difference, Hapy is less expensive per-mile.
 
Wrap
Around that work, there's the usual clearing brush, mowing lawn, etc that comes from living in a house, and spring growth. Our favorite construction contractor was over on Saturday to experiment with the south-facing doorway in the shop. After some large thinking, we are going to put in barn-door style doors, but with fiberglass so the little bit of winter light we get will make it into the building. That's it for this week. Thanks, as always, for following along-

Wednesday, April 22, 2026

Hapy not Spittin Fuel

I managed to get Hapy, the 1972 TDI-powered microbus, over to Justin to get the injection pump re-sealed this weekend. Today's post covers that adventure as well as a quick trip thru a K'Lack (2004 VW Jetta Wagon) issue.
 
Getting There
head seal complete
It has been 2 years since Hapy really went much of anywhere. Most of that time, he sat waiting for attention either in an unknown, but unstartable state or in pieces. Once I had him re-assembled with a new flywheel/ring gear and had a test drive, the original reason for him to have starting problems re-appeared: Injection Pump losing prime. I was able to prime the pump with a MityVac and then crack the injectors to get him running. And, in that way I took him on a short test drive, found some issues with the lights, etc. There remained many other issues, but at least I could get him running, stopping and had my lights so I could drive him an hour and 20 minutes to Justin's shop.
 
The night before our start-of-day appointment, I got Hapy out of the back and filled with B-20 biodiesel ($6.40/gal. same as dinoDiesel. Thanks, Trump). That morning, I filled up with coffee and hit the road. Most of the drive from West Beaverton to Justin's shop is on back country roads with few other drivers on an early Saturday morning and even fewer traffic lights. It was in the 50's (F low-teens C) and clear, making the drive very pleasant. At some point after I fixed the rear speakers, the stereo lost access to 12V so I drove in silence, a familiar scene for Hapy. The road was so easy, the thermostat never opened. I had the cabin heat on, so I may have been pulling just enough heat off the engine to keep the thermostat closed. Based on the UltraGauge, the engine temp was hovering around 180*F so running "cold". When I pulled into town off the country roads, I had a few cases of not finding 2nd gear. I noted that for followup later. When I arrived, Justin and I hung out for a bit before getting started. He has so many interesting projects all going at once, you have to absorb it all. I mean, who puts a TDI in an Audi TT while also putting one into a Rabbit pickup? Love that! The way he scraps discards and re-uses them for the basis of tools is pretty awesome too. He's even teaching himself TIG welding. Small crush, maybe. Okay, fine. He does do some impressive stuff.
 
Injection Pump (IP) Reseal
hammer mod perfecting IQ
Justin had encouraged me to get the seal kit from Cascade German, since they are local-to-Oregon, when we first set the apointment. I had already purchased the deluxe kit from DieselGeek. I didn't understand the difference. These 2 kits definitely vary in their intended purpose, so they have some meaningful differences. The Cascade German version is actually less expensive, but it includes all of the little seals usually replaced when a legit shop does the re-seal. The DieselGeek kit has far fewer seals (just the 2 on top and the head-to-base seal) and it is designed for the home-mechanic to re-seal the pump in their garage without removing the pump from the vehicle. The DieselGeek deluxe kit is more expensive because it includes specialty bits a car owner probably does not have, but are needed for the job. This differentiation is important and your case may lead you to the larger kit even if you do not intend to replace much more than the 3 included in the DieselGeek deluxe.
 
Once Justin discovered the gap, we made-do with the smaller kit. Justin replaced the top 2 seals first and then moved onto the head-to-base seal. Rather than use the included "retraction limiting bolt" and try to fit the new head seal over the top of it, the head was removed, and I held the guts of the pump in-place while Justin cleaned all the surfaces and installed the new seal onto the head. Once installed, he hooked up the VagCom and hammer-mod'd (link to Hammer Mod thread on TDIClub) the injection quantity (IQ). Justin was aiming for 6.0 mg/stk because the engine was cold (54*C).
 
The engine bay was pretty dirty, so lots of time was spent getting the IP clean before we began as well as afterwards when the whole engine got a cleaning. After it dried off a bit, we let the engine idle and we looked for leaks. None found. Justin did ask about how the starter was mating to the flywheel. It does sound loud, like it may not be meshing quite right. I'll need to remove and reinstall the starter and the starter adapter to see if I can get things to sit right. The original adapter and starter that I put in just worked for years. I would expect the new-also-stock starter would fit the same. Since this is a new adapter, that is actually designed for the application, versus one I dremel'd to fit, I would think it would fit better. It's a puzzler, but one I will consider carefully as I remove/reinstall (R&R) the starter to get it to hit the ring gear more cleanly.
 
Getting Home
If there is anything we have learned over the years about Hapy, its that he loves going places and really does not like going home. How many times have I left home and the road trip to 4 Peaks or some camping spot went great and the drive home was either very challenging or partially performed by a flatbed? Too many. This trip was no different. At first, Hapy ran great. The engine was responsive and stayed cool. Somewhere around McMinnville a charged air pipe popped off, leaving me running naturally aspirated the rest of the drive home. This served as yet another reminder to never leave home with Hapy without some tools. While the turbo is great for the overall power-band, its absence is really noticeable when trying to leave the line and get up to traffic speed. Now that it was about noon on an absolutely stunner of a day, the roads were busy where they had been empty a few hours before.
 
By the time I was approaching the Dundee Bypass, I was having increasing difficulty finding 1st and 2nd gear. Sometimes, one or the other would be right there. Other times, it was a "can't find it, grind it" experience. This persisted all the way home, forcing me to sometimes leave a stop line in 3rd. When you add in the no-turbo, I had some dissatisfied fellow travelers around me. I did get home, however, and I drove Hapy all the way into the shop so I can chase these issues.

K'Lack
After having something to eat, I switched over to K'Lack, the 2004 TDI Jetta Wagon with a BEW motor. It had been throwing a crank position sensor error, lighting up the check engine light (CEL), preventing it from passing smog. I had ordered a replacement from Cascade on Thursday, and it was in the morning mail on Saturday when I got home from Justin's. The removal/replacement of these is not complicated (remove bolt, unplug from harness, install is reverse), but getting to the sensor and the weird bolt head complicate things. The sensor sits right behind the oil filter on the front, when the engine installed transverse like normal. The bolt head is a 9mm 12-point. Half of my sockets are 6-point and the other half are 12's, designed, I think, for easier application onto hex bolts. In this weird case, that socket set perfectly onto the 12-point bolt head. With the right socket, short extension and ratchet the bolt comes out fairly easily. The plug end is fitted into a metal tang, but otherwise once unplugged, the whole thing can just get dropped through the gaps onto the ground.
 
To install, I plugged it in first and then covered the sensor with a rubber glove to lower it past the engine ick and then below the car. Could I have cleaned the engine bay before starting? Yes. But then I would have been lying in mud since the car was on my front lawn, not back in the shop and I didn't want to lay in a puddle. At this point, I found having another person to be your eyes is very helpful. I got under the car, un-gloved and suspended sensor in hand and had Boo tell me east-west, up down until I was able to send the sensor into the hole. By doing it in this order, the sensor wanted to be oriented such that the bolt holes lined up naturally. I sent the bolt thru, tightened with the socket/ratchet combo and I was done. Since I cleared the code we need to run a few cycles until it is ready to smog.
 
For the legal-minded, Oregon cops are interested in registration violations after years of looking the other way post-CoViD. K'Lack got a registration-violation ticket while legally parked in downtown Portland. Drivers beware.
 
Hapy Wrenching
Feeling confident, I switched back to Hapy, and re-connected the charged air hose. As I suspected, it was one of the rubber-to-metal bits. I cleaned both the outside of the metal pipe and the inside of the rubber with brake cleaner so they were more apt to stay together and then tightened the clamp down.
 
I next wanted to chase why the lower gears were sporadically missing. I checked the front of the transaxle to see if it was out of position at all. Nope. Right before Boo and I bought this house, I bought a Gene Berg shifter. The new-at-that-time seats were higher than stock, moving the approximately-stock-length Scat gear shift further away. The Gene Berg shifter is a few inches longer, so I figured there would be less leaning. I had not gotten to installing it before the house was bought and life took a turn. Anyway, at this point I looked at the Scat shifter I had installed, probably over 15 years ago and slid the vinyl boot up the shifter. The plastic bits on either side of the shifter appeared to be allowing more play than I remembered. Hmm. Then, I looked at the rest of that mechanism. It was very rusty, especially the foot that rests on the floor. I shot the bolts with Kroil and after waiting a couple of minutes, removed them with a 13mm spanner/socket combination.
 
rust under shifter
The floor under the shifter had meaningful rust to match the rust on the shifter foot. I don't know how much play was created by the plastic bits, nor how much may have been introduced by the rust. I do recall, however, that the Scat shifter instructions did not account for adjusting the placement of the shifter front/back nor left/right. When looking at the foot profile, it looks very much like it is designed to sit squarely in the oval without any adjustment at all. I don't know if this was a terribly good design, but I will be installing the Gene Berg shifter which does allow for adjusting. I cleaned up the rust dust, shot the floor and the shift-rod end with brake cleaner and got everything as clean as I could. Then, I painted the area with Eastwood's Rust Encapsulater (the new stuff is even better than the original) and called it a day. I still need to treat from below. I shot the picture on the right here as I was almost done applying the paint.
 
Wrap
Well, that's where we stand right now. I have been in and out of the shop a few times since Saturday and there is not a single drop of fuel on the floor under Hapy. So, we can close the book on the IP leak. I intend to complete the shifter swap and then R&R the starter next. I hope that will be the end of both issues, but I suspect there will be more to do than that. Then, of course, there are all the other things like a fuel level gauge, the radio, and the diesel heater just off the top of my head. There are many incomplete items on Hapy. Now that I have a mostly-inside (one doorway remains), concrete floor'd space to work, my desire to work on these cars has really kicked into a new level.
 
Thanks, as always, for following along and more next time-

Wednesday, April 15, 2026

Building a Shop - Doors

Ia accept that putting a garage door on your shop is barely car-content, but it is the big deal around here, and it is at least tangentially related to cars. Recall, the shop was designed with 4 openings: on the North, the big door and a person door; facing West, a barn door and facing South a to-be-determined door. I lightly described the barn door in the Ghost of GoRo. Today's post is about getting a big door for the front of the shop and all the stuff around that.
 
Before I begin, for my US readers, happy tax day. I recognize there are very curious ways this administration and his congress are choosing to allocate money, and today of all days, that "curious" feels more acute. You may not be able to influence their choices, but you can choose to vote with your wallet every day. Please direct your purchasing choices into small businesses. Those mom and pop operators are your neighbors. When you invest in them you are investing directly into your community, and not into some corporation which takes from it.
 
Measure Twice
This is so obvious and yet, this was almost my biggest mistake. When I first was designing the shop, I had the front of the shop (facing north) almost completely open for a massive door: 6 meters / 18 feet wide by 3.3 meters /10 feet tall. My thought at the time was that 6 meters would easily allow me to move 2 cars side-by-side without having to get either too deep into the shop. Like, I could have one sticking halfway out and still get a car in. This was great thinking until I decided I wanted a way to get in/out through a "man" (I say "person", but I'm not pronoun-hostile either) door. I also wanted this facing North, next to the big garage-style roll-up door. This way I could leave the big door closed and still come and go through a door with a lock on it. Consider the barn door is locked from the inside, and that was always the plan. I have no idea what the southern door will be like, but it may not have an externally-facing lock on it.
 
no wind inside
Anyway, fast-forward to after it is built and I am looking for a tracked roll-up door. After spending weeks looking for a 18' x 10' door, I have a site visit by a local door company (Overhead Door of Portland) who has a used door that big. We run the tape and sure-enough the opening is 10' high, the clearance above is adequate. Then we check the door width and it's only 16' (5 2/3m). Duh. When I added the person door, I reduced the size of the roll-up door and completely forgot. Ultimately, this saved me a bunch of money, though, because a standard residential tracked roll-up door is 5 2/3m (16 feet). When I say a bunch of money, the used door he had would have to cost me $14k US including install and an opener. The larger opening also would have pushed me into a commercial-grade door, so it would have weighed nearly double the residential door.
 
Patience Pays
open, windy inside
With the more accurate measurement, the fine folks over at Overhead Door of Portland dug into their stock of used doors. After a few weeks, they had a suitable door. Boo and I want a glass door, to maximize the light coming on for cold daytime work (think: winter weekends) and to not block overhead lights when it's open. We both also thought that a clear door would more closely approximate an old filling station look that we both had romanticals about. These glass doors, though, are less common and more expensive. The door they have is undamaged, but whoever had installed it chose to mask off the glass and then rattle-can paint the doors and rails with black Rustoleum paint. That decision would have been totally fine, had they prepared the surface for paint. At bare minimum the doors needed to be scuffed with 300-grit to 400-grit sand paper (or a red ScotchBrite pad) so the paint would have something to bite into and then wiped down. They did not and the paint did not. Instead, the paint is flaking off and is not presentable to most. For our purpose: make opening clear, yet lockable while looking old-Skool... it is perfect. We may change our minds and fix the paint, but for today, we are happy with it.
 
Car Mad Dash
Hapy's spot
As is so often the case, this was a full-on hurry up and wait. Well, really, it was more of a wait and then hurry-up. I have been looking for a door since the shop was built and now that we found one, the install was planned for less than a week later. From my prior post, you know that Oliver is against the east wall, right up against the big door opening. And, he was not running. Next to him is Hapy, barely jutting out the big opening and barely running. I needed to get both cars out the way and the lane way clear so they could get in there with the doors and equipment to get the door installed.
 
Getting Hapy out was easy: re-prime the Injection Pump with the MityVac, crack the injectors, pop the starter to a count of 5, re-tighten the injectors, start and back him out. This took less than an hour and I parked him in his longer-term designated spot where we can more easily visit and drive him. Yeah, I said visit; he's family.
 
Oliver drove!
Moving Oliver was a bigger deal, but only because I made it so. I wanted him to leave the shop under his own power. So that meant getting him running. In my last post, I described solving his fuel system. I don't know if it was insufficient patience or if I flooded the carb, but he would not start that day. A week later, and I have Hapy out of the way, I was ready to push Oliver out if I had to. First, I checked his spark plugs. They smelled like gas and were fairly black (fuel mixture probably too rich). I hit them with a wire brush and then re-set the gaps (0.033", internets recommend between 0.025" and 0.038") depending on lots of factors. I turned the key, got the fuel pump to prime and then quiet way down. At the carb with my hand, I "pumped" the accelerator a couple of times. At the wheel, I pulled the choke and tried to start him. After a few seconds, he started to act like he wanted to and after a few more tries, he fired up and held idle. This was the first time he ran since I rebuilt the carb, so an historic moment. Attempts to vary the engine speed with the accelerator pedal were fruitless, so I idled out of the shop, down the inclined gravel drive, and parked him in front of the person door. I was able to confirm that the throttle cable was junked. It would not stay on the pedal arm and then I was unable to move it consistently by hand. I'll be replacing that soon.
 
Final Prep
installers getting started
With the cars out of the way, I could get the last bits done for the door installers. I had strung outdoor patio lights around the inside of the shop, extending across the large door opening. So, half of that strand needed to come down. Last, I swept the floor which had not been really looked at since I moved the cars in last fall. With Oliver and Hapy out of the shop, I was able to really appreciate the size of my new workspace. It's really nice, and I will need to make a focused effort to leave myself room to work by not housing all of the cars inside all the time.
 
Door Install
The 2 installers from Overhead Door of Portland arrived as-scheduled around 10AM. They backed most of the way down the lane-way so the distance to carry the panels and runners was shorter. In half an hour, the doors were off the truck and positioned for installing (picture on the right). By 1130AM, 4 of the 5 door panels were installed on the runners and they were a-fixing the runners to the building. By 1PM, the door was in, the runners set, and the spring installed. Within the next hour, the install was complete, and Chris and Chase were showing us how the various controllers worked. With the door open, obviously, its almost like being outside. Well, its exactly like it was before the door was there: Full wind and misty rain on my face. Overhead, once lights are installed, the door will not block the light from reaching us beneath. That's huge. When the door is shut, the sound, wind and rain all stop. I did not expect the degree to which the air movement and sound would change. It is significant.
 
Wrap
Well, that's it for today. Next, I will be replacing the rear brakes on K'Lack (2004 Jetta TDI driven by my niece), replacing the throttle cable on Oliver and bringing Hapy over to Justin's to have the Injection Pump resealed. I don't know if any of those are really blog-post-worthy. Summer is coming, and having a safe vehicle (or a few safe vehicles) for Summer adventures starts now. As always, thanks for following along-

Tuesday, April 7, 2026

Oliver Fuel Fun

Boo had to work on Easter, so I had a Sunday to work with. Knowing others around the neighborhood were celebrating Easter with their families, I wanted to keep my noise and smoke to a minimum. So, I started slow, throwing Oliver onto a charger and then doing inside stuff. By 11, I was mowing the front lawn with the electric mower. With hand tools, I fixed the gates to the fence by lowering the little swivel wheels and re-setting the patio block they set on. Now, the gates sit mostly level and mostly vertical. By 2PM, most of the family gatherings were breaking up, so I felt I could make engine noises and such. So, I headed out to the shop. Engine noises. Ha. Such optimism.
 
No Start
fuel works
I am sure this comes as no surprise, but my first attempt to start Oliver was not successful. I really didn't expect it to, tho. I had a little over a gallon of gas in a jug that I poured into the tank, but I noticed that the fuel pump noise never lessened. So, as I walked to the rear of the car, I expected there would be no fuel in the filter. And there wasn't. The series of things the fuel needs to pass through before arriving at the pump is: fuel level sender / pick up tube -> flexible fuel line -> clear plastic fuel filter -> flexible fuel line -> fuel pump. From there, it travels, at pressure, thru another flexible line, through a short section of 90* hard line, more flexible line and then to the hard line that runs along the frame to the engine compartment. That's a lot of junctions. I started at the pump, testing with a MityVac vacuum pump, working my way back towards the tank. In retrospect, it would have been smarter to work my way forward from the tank all the way to the carb. Lesson learned.
 
Fuel Shower
upper one is bad
One of the short hoses was bad, but there was nothing visibly wrong with it. The picture on the right here is of those 2 lines. The top one cannot hold vacuum; the lower one can. This serves as a great reminder for those driving gravity-fed fuel system'd vehicles like the old VW bus. Fuel lines fail, sometimes not that long after you've installed it and sometimes you can't tell from looking at them. For a gravity feed system, you discover the leak after you've filled your tank, and it gushes onto the ground it you're lucky. Onto your hot exhaust if you're not.
 
While looking for the cause, I cracked the fuel level sender on the tank to confirm that I had enough fuel. I did. Once the one short line was replaced, I went up front, turned the key and started looking for another leak. I did not have to look very far. Immediately forward of the fuel pump, I had fuel going everywhere, running down the rear differential.
 
I concluded that it was another short hose, but noticed that the combination of short hose, weird 90* hard line, longer hose made little sense. I think I did that when I installed the fuel pump because the outlet of the new fuel pump was not clocked the same as the original and I didn't want a kink in the hose. If I remember correctly, I had already cut that longer hose, and solved the wrong problem. Or solved the right problem the wrong way. I think, that 90* bend was from the original system to go from the sender to the pump, and in this installation, I have a clear plastic fuel filter serving that function. Regardless, I corrected this time with a longer hose that runs from the pump to the long hard line. The longer hose was long enough to have a gentle arc, preventing a pinch in the line I was probably trying to avoid with the weird combo of parts. In the bottom picture, you can see that I have a small fuse for the fuel pump. This was not there stock, but I felt that with so many things living on the switched circuit, having a fuse around the fuel pump was probably a good idea.
 
Still No Start 
fuel pump
With the rear end lines set, I turned the key again, and the fuel pump quieted down after a few seconds. I looked under the car and no puddle was forming. There was not a drip at all. I went to the engine compartment, and there were no leaks there either. So, I tried to start it. No love. By now, it was approaching 5PM, and I had to get dinner started. But first, I wanted to know if the hard line was blocked or if there was fuel at the inlet on the carb. I removed the fuel line and gasoline dribbled out. Win. We have fuel at the carb. I put everything back together. Before heading inside, I checked the lights and hazards to give myself a little "well that works" energy before calling it a day.
 
Wrap Up
That's as far as I got on Sunday. After the random home-repairs, I had left myself more than enough time, had Oliver actually started, to give him a deep cleaning. That still needs doing, but first I need for him to run. I rebuilt the carb a couple of years ago, and the engine ran with it on there, so I don't think the issue is fueling, but it still could be. I will start with the spark plugs next time, and confirm I have spark. It is absolutely possible that something worked free during the move into the shop. If that does not bring me the start I am seeking then I will re-examine the carb. Maybe some gas residue became a thin varnish holding the bowl float, or is clogging a jet or something. 
 
That's all for now. Thanks, as always, for following along- 

Wednesday, April 1, 2026

Returning to Oliver

The last week or so has been busy with lots of not-car stuff. We have had our young niece over a bunch while her mom had surgery on her wrist, and a bunch of social events. Of course, with the return of spring comes the return of recurring yardwork as well. So, I have not had the dedicated time for wrenching that I always seem to think will be available. I was able to get out to the shop for a few hours on Sunday, though. I focused on Oliver, the 1978 MGB, letting Hapy ('72 VW microbus) sit until Justin has his time with the injection pump in April. The rate at which the price of diesel fuel is climbing (passed $6US/gal around the corner), I may find that it costs more to fill his tank than to pay Justin for his time. That's totally upside-down. Anyway, back to wrenchin.
 
Voltage Gauge
remember Oliver?
I installed a Smith voltage gauge into Oliver where the original analog clock used to sit. The clock didn't really work very well, and it ate voltage from the battery when I let him sit for too long. This made the clock less accurate, leading me to pull the positive cable off the battery while not in use. This led to the clock being completely worthless. So, I pulled it out and swapped in the voltage gauge. It seemed like a valuable bit of info to have, but I had wired it into the "purple" or always-hot circuit. Like the clock, the voltage gauge slowly drained the battery down, albeit not as quickly. So, again, I pulled the positive cable while not driving. I changed that on Sunday.
 
Bearing in mind that any entry back into working on cars may not seem like a big deal to regular wrenchers, but I have really not done much car stuff in over a year. So, any steps taken are a big deal. Removing the gauge was simply unwinding the knurled nut holding the rear support and the gauge flopped forward out of the dash. I removed and taped-off the "purple" wire and started seeking a viable switched "green"source to tap into. Switched is available at a few spots, but I decided to run a dedicated line from the fuse box instead. I could say I did that to remove variables or variability in the voltage signal. The truth is that Oliver is parked so close to the side wall of the shop that getting in and under the dash was virtually impossible. I was not going to just start grabbing an unplugging things.
 
Smith voltage gauge
Running another wire is simple enough. I started at the gauge and worked my way behind the dash, center console, and glove box to the firewall pass-thru. From the pass through within the engine compartment, the bundle of wires run along the left fender to the fuse box. I tied the new wire into the existing green bundle and tested continuity with the multi-meter. Success! I installed the gauge, hooked up the battery and tested by turning the ignition to "run". The voltmeter slowly crept up and I could hear the fuel pump banging away. I recall that it used to get quieter with fuel in the pump. Satisfied, I turned off the key and looked for any other parasitic drain on the battery. The wires in the engine compartment need some containment. I am not liking the scattered multi-colored angel-hair look in the picture below right.
 
Battery Drain?
technicolor angel hair pasta wiring
Testing for a parasitic drain on your battery ought to be relatively straight-forward. Disconnect one cable. Set your multi-meter to test for Amps and then place one probe on the battery post and the other on the cable end. All 0's? Switch to milli-amps and try again. According to the internets, if the drain is less than 50mA, it is not enough to drain your battery. I got 0mA, which, honestly, I do not believe. I tested it multiple times, and even after cleaning the cable and the battery post, I still got 0mA. So, I checked voltage across the 2 posts (12.08V) and left the cables attached. I figured if the voltage drops overnight then my battery-drain test will be proven faulty. I have since tested the voltage the last 2 days. The battery loses 0.02V overnight, which I think I can attribute to the stereo. Regardless, I will need to add a float charger.
 
Red Rollie
new lock, locked
I have this old red Kennedy tool cabinet we call "Red Rollie". It houses a bunch of tools, and for most the nearly 20 years that I've owned it, the lock didn't work. Well, I didn't have a key for it. We got the cabinet at an estate sale without the key. Anyway, some tools were stolen from my next door neighbor's yard a few months ago, so that changed our vector regarding the shop. We were perfectly fine using it without doors, but I can't leave entire tool cabinets unlocked if thieves have found our quiet little neighborhood. While I think the theft next door was an inside job (they run a construction business out of their home), one can never be too sure. So, I found a lock that fits this old Kennedy cabinet (Kennedy 80403 High Security Tubular Lock), and replaced it.
 
Replacing one of these locks is actually easier than on newer cabinets. The lock is held on with a U-shaped tang that slides off to the side. The hard part is you can't see anything. With my fingers I was able to determine which direction the tang needed to slide to be removed (facing the cabinet, slide right), and then set a stubby slotted screw-driver against the lip of the tang. It only took one well-leveraged push to get the tang removed and the lock to pop out. To install, orient the lock so the little inner divot on the outside facing part of the lock where the key goes in is facing down (unlocked). Set the lock into the hole with one hand while guiding the locking rod into the rectangular hole on the back of the lock. Then, push the U-shaped tang in place to hold it.
 
Red Rollie
This worked great, and effectively locked the top 2 drawers. The 3rd drawer down, however, had been bent where the little hook pokes out the back. To remedy, I got a framing hammer and a 1/2" ratchet extension and beat on it until it was more-or-less flush with the rest of the rear of the drawer. For years I wondered why that drawer always set deeper into the cabinet than the others. Now I knew. Once the drawer had been persuaded, the drawer fronts lined up and that 3rd drawer locked as well.
 
Wrap
That's how I spent my Sunday afternoon. The shop still needs the 2 largest doors, but my tools are secure, and I am really starting to get comfortable in there. For example, there was a period of time while working on Oliver that the skies opened up and it started pouring rain. I never felt it. In fact, I could only hear it hitting the trees. The insulation on this shop stops the sound of rain on the steel roof. I absolutely did not expect that.
 
That's it for today. Next week is Easter, so I may not get out to the shop for much. I hope to put a little gas into Oliver and at least back him out to where I can give him a deep cleaning.